So, I blew my twin turbo'ed motor at a track event.... 7500rpms and a cylinder disintegrated. the rod essentially slapped 2 massive windows on each side until the engine wound
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08-09-2020, 11:32 PM | #1 (permalink) |
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Join Date: Jun 2017
Location: Denver
Posts: 135
Drives: 15' 370z SpTech 6MT
Rep Power: 3363 |
Blowing my TT'ed motor and swapping a new one back in
So, I blew my twin turbo'ed motor at a track event.... 7500rpms and a cylinder disintegrated. the rod essentially slapped 2 massive windows on each side until the engine wound down. The shrapnel i found in the pan and all over the car was surreal.
I made some videos about my journey to swap motors and re-install the turbo kit ( along with some other mods ) in my garage. I still have a couple of installments, but im almost done. Ill add them in as I go.
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AAM tt'ed // Soon: Moving back to the East Coast Last edited by Girald; 08-22-2020 at 12:09 PM. |
08-15-2020, 12:10 PM | #2 (permalink) |
Enthusiast Member
Join Date: Jan 2018
Location: Netherlands
Posts: 280
Drives: 2010 370z MB 6MT
Rep Power: 3786 |
Too bad man but happy you got it fixed.
What boost pressure level and fuel you ran? Sent from my SM-G973F using Tapatalk
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Instagram: Boosted_Fairlady |
08-17-2020, 12:04 AM | #3 (permalink) |
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Join Date: Jun 2017
Location: Denver
Posts: 135
Drives: 15' 370z SpTech 6MT
Rep Power: 3363 |
I set the fuel pressure per tuner's request... Fuel pressure is a moving target since the fuel pressure regulator adjusts pressure via the vacuum pressure. Maintaining a strong fuel system to accommodate the need is always key.. Im running a Walbro450 with a fuel return and a pump speed controller. and sand alone wiring and relays to allow for adequate power. At the time of the incident, the tank was about 85% full, so a starvation condition is out of the realm of speculation
The system has been monitored, logged and video'ed from the gauge in the engine bay, and a ll is solid... so the fuel pressure is not a factor. When I pulled the motor out, all of my vacuum lines were intact. In reality, you dont stare at all of your gauges when bulleting down a track. You can have warning lights go off, but you arent going to analyze anything until after you stop the car, since the goal is to get down the track safely. I wasnt logging at the time of the incident, so who knows.... As for boost, i hadnt modified the boost from the tune map.It was a fairly agressive tune and I was at redline when she went boom... I chalk it up to : something had to give, and 1 piston simply had enough..... This car has been open track'ed, drag raced, top ended, run through mountain and canyon passes, autox etc. This car is no pleasure tub. It works for its space in the garage. Its not a daily driver, though i do drive it to work sometimes. 20/20, i prob could have dialed the boost back since I has that option, but I sent it like any self respecting Z owner would Moving forward, im going to have the tuner fine tune this map to accomodate any variables in the engine swap, to get me going, but, basically the same tune.. Im going to dial back the car in the interum though until I can put the $$$ to build the motor. After that, cleared for take off with motor to spare...
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AAM tt'ed // Soon: Moving back to the East Coast Last edited by Girald; 08-19-2020 at 07:50 PM. |
08-17-2020, 12:16 AM | #4 (permalink) |
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Join Date: Jun 2017
Location: Denver
Posts: 135
Drives: 15' 370z SpTech 6MT
Rep Power: 3363 |
Just an update:
ive got most of the car done, just need to put the radiator housing back and finish up.. i took a break ( sometimes you need to step back) But, im back at it tonight... Some time this week, i should be ready to hit the start button. After that much work, im a bit anxious hoping that i got the inaccessible parts torqued down right and i didn't miss anything... leaks are also a concern as always, Ill drop some videos once the nose is back on.
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AAM tt'ed // Soon: Moving back to the East Coast |
08-17-2020, 06:45 AM | #5 (permalink) |
Enthusiast Member
Join Date: Jan 2018
Location: Netherlands
Posts: 280
Drives: 2010 370z MB 6MT
Rep Power: 3786 |
Good to hear you are progressing. But how much PSI did you run? Im asking because i see a fair lot of boosted engines blowing up lately, including my own. Trying to understand the limits a bit better.
Sent from my SM-G973F using Tapatalk
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08-18-2020, 09:54 PM | #7 (permalink) |
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Join Date: Aug 2012
Location: Albuquerque NM
Posts: 577
Drives: 2010 Roadster 7AT
Rep Power: 307 |
I ran mine hard (drag racing) for 3 years at 15-16psi and it never failed.
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F.I. Stage 1 Twin Turbo #48 | E85 FlexFuel | Built 7AT | F.I. 34 Row Oil Cooler | F.I. Flex Plate | F.I. 19 row Trans Cooler | MT ET Street S/S | ECUTEK Tuned by Seb | RPM Roll Bar |
08-19-2020, 07:48 PM | #8 (permalink) |
Base Member
Join Date: Jun 2017
Location: Denver
Posts: 135
Drives: 15' 370z SpTech 6MT
Rep Power: 3363 |
Shes running now... just a cylinder6 misfire atm... going to pull and swap plugs and see what happens... If its injectors ill have to go to a shop that tests and cleans out injectors.
Ill drop a youtube video tonight... most likely, ill have 1 more after this ( since im working on the interior as well.. UPDATE: haha found a wire out of the connector on the fuel rail.. easy fix ( thank goodness ) have to let the car cool down and ill fix it POST SCRIPT: took her out for a weekend drive, dumped all my oil on to the freeway... at least i had it shut down right after. the oil pressure hit zero;; ( oil cooler hose decided to die... I had extra, so this morning got fixed and took another drive and all is well.. cant wait to get the all clear from seb, and its back to shennanigans
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AAM tt'ed // Soon: Moving back to the East Coast Last edited by Girald; 08-23-2020 at 01:26 PM. |
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