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To day I send 2 hours on the dyno to test 2 mods that I did in 2011. Normaly I always do a dyno session after any power mod but
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#7 (permalink) |
A True Z Fanatic
Join Date: Oct 2009
Location: Canada
Posts: 1,156
Drives: 370z
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To day I send 2 hours on the dyno to test 2 mods that I did in 2011.
Normaly I always do a dyno session after any power mod but since last year I was plaged with the ECU pulling timing and not knowing it untill I blew the tranny on the drag strip. The flywheel was badly cracked, which we think it was affecting the knock sensor to not be happy thus pulling timing ! It was difficult to have much of any consistense pull after pull but since the flywheel got replaced, I do not have any problem with that ! Soo today was to confirm 2 mods. 1= HR vs VHR intake manifold (you can see my picture when I did the conversion) ![]() - 2= Throttle Body OEM stock @ 60mm VS bored at 62.5mm The AFR were ajusted before the recording pull. ![]() |
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