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Add me to the list. At 10k miles my motor went down with TT and oil cooler, dual intercooler setup. Boost was set to 10psi and WHP was just over
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#1 (permalink) |
Base Member
Join Date: Jul 2012
Location: California
Posts: 57
Drives: 2012 G37 IPL 7AT TT
Rep Power: 13 ![]() |
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Add me to the list.
At 10k miles my motor went down with TT and oil cooler, dual intercooler setup. Boost was set to 10psi and WHP was just over 500. My check engine light came on and the engine began to run very rough. I had it towed and the code the engine threw was a valve error. Long story short, I now have a built engine after a long wait and Many dollars invested I hadn't planned on. What can I say? You play with fire, you can get burnt!
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2012 G37 IPL 7AT | GTM Stage 1 Long Block | GTM Stage 1 Garett TT | Blitz SBC typeR Boost Controller | GTM Stage 4 Transmission | Tial BOV | Fast Intentions exhaust | GTM 8qt Oil Pan | 583whp/484trq @ 13psi |
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#2 (permalink) | |
Base Member
![]() Join Date: Sep 2010
Location: USA
Posts: 138
Drives: 2011 Infiniti G37S
Rep Power: 15 ![]() |
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Also, wasn't your car the test vehicle for the 16G MHI Kit (in the link below)? GTM Performance Engineering: GTM TD05 16G Test Results 91 Octane 7AT |
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#3 (permalink) | |
Base Member
Join Date: Jul 2012
Location: California
Posts: 57
Drives: 2012 G37 IPL 7AT TT
Rep Power: 13 ![]() |
![]() Quote:
It seems it was the valve that bent somehow. Sam said possibly over-rev or something. So ultimately I went stage1 long block with forged internals. In the end I ended up with the Garrett turbos and a stage 4 tranny so I wouldn't face any more issues.
__________________
2012 G37 IPL 7AT | GTM Stage 1 Long Block | GTM Stage 1 Garett TT | Blitz SBC typeR Boost Controller | GTM Stage 4 Transmission | Tial BOV | Fast Intentions exhaust | GTM 8qt Oil Pan | 583whp/484trq @ 13psi |
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