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How many went FI and blew a motor?

Add me to the list. At 10k miles my motor went down with TT and oil cooler, dual intercooler setup. Boost was set to 10psi and WHP was just over

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Old 10-23-2013, 08:59 AM   #1 (permalink)
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Add me to the list.

At 10k miles my motor went down with TT and oil cooler, dual intercooler setup. Boost was set to 10psi and WHP was just over 500.

My check engine light came on and the engine began to run very rough. I had it towed and the code the engine threw was a valve error.

Long story short, I now have a built engine after a long wait and Many dollars invested I hadn't planned on.

What can I say?
You play with fire, you can get burnt!
Mkai0 and elperuano like this.
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2012 G37 IPL 7AT | GTM Stage 1 Long Block | GTM Stage 1 Garett TT | Blitz SBC typeR Boost Controller | GTM Stage 4 Transmission | Tial BOV | Fast Intentions exhaust | GTM 8qt Oil Pan | 583whp/484trq @ 13psi
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Old 10-23-2013, 01:26 PM   #2 (permalink)
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Quote:
Originally Posted by Wattles View Post
Add me to the list.

At 10k miles my motor went down with TT and oil cooler, dual intercooler setup. Boost was set to 10psi and WHP was just over 500.

My check engine light came on and the engine began to run very rough. I had it towed and the code the engine threw was a valve error.

Long story short, I now have a built engine after a long wait and Many dollars invested I hadn't planned on.

What can I say?
You play with fire, you can get burnt!
I'm really sorry to hear this. I hope that you can get your car back on the road again soon. Did anyone figure out what caused the valve error and the subsequent engine failure?

Also, wasn't your car the test vehicle for the 16G MHI Kit (in the link below)?

GTM Performance Engineering: GTM TD05 16G Test Results 91 Octane 7AT
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Old 10-23-2013, 09:55 PM   #3 (permalink)
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Quote:
Originally Posted by showme99 View Post
I'm really sorry to hear this. I hope that you can get your car back on the road again soon. Did anyone figure out what caused the valve error and the subsequent engine failure?

Also, wasn't your car the test vehicle for the 16G MHI Kit (in the link below)?

GTM Performance Engineering: GTM TD05 16G Test Results 91 Octane 7AT
Yes my car was the original. Then it had the problem so we rebuilt it when we found out it needed to be cracked open to fix the problem.
It seems it was the valve that bent somehow. Sam said possibly over-rev or something.
So ultimately I went stage1 long block with forged internals.
In the end I ended up with the Garrett turbos and a stage 4 tranny so I wouldn't face any more issues.
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2012 G37 IPL 7AT | GTM Stage 1 Long Block | GTM Stage 1 Garett TT | Blitz SBC typeR Boost Controller | GTM Stage 4 Transmission | Tial BOV | Fast Intentions exhaust | GTM 8qt Oil Pan | 583whp/484trq @ 13psi
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