Originally Posted by Footloose301 Did you go back to MySpace? Never touched that slime. On topic: woot.
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02-07-2013, 08:06 PM | #287 (permalink) |
A True Z Fanatic
Join Date: May 2011
Location: Midland, TX
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Drives: 11 370Z PW M6
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I'm not even paying attention to what's going on at work cause I keep checking for uploads
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10secWS6 IF YOU CAN'T SWING IT THEN DON'T BRING IT! Check out Domestic Performance C.C. |
02-07-2013, 10:13 PM | #289 (permalink) |
Track Member
Join Date: Sep 2012
Location: Kansas City
Posts: 878
Drives: '11 370Z SPT 6MT BLK
Rep Power: 25 |
For those that aren't following FI on Facebook (https://www.facebook.com/FastIntentions)
Tony just posted a picture of the car strapped down on the dyno. |
02-08-2013, 12:28 AM | #290 (permalink) |
A True Z Fanatic
Join Date: May 2011
Location: Midland, TX
Posts: 3,884
Drives: 11 370Z PW M6
Rep Power: 23 |
Stupid company laptop doesn't let me get onto FB
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10secWS6 IF YOU CAN'T SWING IT THEN DON'T BRING IT! Check out Domestic Performance C.C. |
02-08-2013, 01:33 AM | #291 (permalink) |
The370Z.com Sponsor
Join Date: Feb 2009
Location: Simi Valley, CA
Posts: 2,989
Drives: 2010 GT-R/2007 F-250
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Update,
Just finished dyno testing the full 2.5" set up. The fuel pressure is dropping in the high end and we are going to sort that out. Here is what we have so far. 91 Octane: 469 RWH 382 FT LBS of Torque Roughly 7-7.5 PSI The boost is fluctuating between 6-7.5 LBS. We are currently running it on strictly wastegate spring pressure with no boost controller. The timing is conservative because we only have 91 Octane and do not want to detonate, obviously! Currently we are strapping the car down and testing it with stock cats and the full 2.5" CBE. Not expecting big numbers in this form and we are strictly doing it out of curiousity and to apease the community. After this is complete we will take the full exhaust off and slap on the full 3". At that point it will get tested again tonight on 91 octane. Tomorrow once we can troubleshoot the slight fueling issue, we will turn the boot up on VP Motorsport 103 octane. Here is what we can take away from this so far. At this PSI level we are not even close to utilizing the potential of what the GTX 28-67 turbo can do! The innercooler setup is proving to be extremely effiecent. After 13 runs we in fact made more power every time. The innercooler is not heat soaking and the IAT's (Inlet Air Temps.) are holding steady in the low 80's. The boost is ramping in fast and hard. The curve is very usable in the low end and mid range. I will keep you posted shortly with another update. Thanks, Tony
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Follow us on Facebook: Fast Intentions Inc. Phone: (805) 522-FAST (3278) Email: tony@fastintentions.com www.fastintentions.com "FUELED BY PASSION" |
02-08-2013, 01:44 AM | #292 (permalink) | |
Base Member
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Location: SD & LA
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Quote:
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02-08-2013, 02:04 AM | #294 (permalink) |
A True Z Fanatic
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Location: Keystone state
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Nice Solid number's Tony cant wait to see the graph and 3 inch exhaust results.
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Driven Motorsports Single Turbo 7675 T4 1.32 A/R 995WHP 780TQ |
02-08-2013, 02:09 AM | #295 (permalink) | |
The370Z.com Sponsor
Join Date: Feb 2009
Location: Simi Valley, CA
Posts: 2,989
Drives: 2010 GT-R/2007 F-250
Rep Power: 685 |
Quote:
91 Octane 431 RWH 355 FT LBS of torque 6.5-7.2 PSI Still very respectable for stock cats! Again, no boost controller. Just straight wastegate spring pressure.
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Follow us on Facebook: Fast Intentions Inc. Phone: (805) 522-FAST (3278) Email: tony@fastintentions.com www.fastintentions.com "FUELED BY PASSION" Last edited by F.I. Inc.; 02-08-2013 at 02:12 AM. |
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02-08-2013, 02:54 AM | #297 (permalink) |
The370Z.com Sponsor
Join Date: Feb 2009
Location: Simi Valley, CA
Posts: 2,989
Drives: 2010 GT-R/2007 F-250
Rep Power: 685 |
Update,
No 3" tonight. Got shut down by Johnny law. Too much noise, too late in the evening. Will get back at it tomorrow. As of now it looks like we are going to make the track Saturday! Stay tuned... Thanks and goodnight. Tony
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Follow us on Facebook: Fast Intentions Inc. Phone: (805) 522-FAST (3278) Email: tony@fastintentions.com www.fastintentions.com "FUELED BY PASSION" Last edited by F.I. Inc.; 02-08-2013 at 03:50 AM. |
02-08-2013, 04:05 AM | #300 (permalink) |
A True Z Fanatic
Join Date: Jan 2009
Location: Socal
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Had a great day today Tony. You guys continue to surpass my expectations. Cant wait for tomorrow and saturday.
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638WHP 541WTQ @ 13.5PSI
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