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Hey guys wondering if anyone is having problems with their sc stage 1 or 2, at 7100 rpm my boost and power just plummet. It is about *100 whp and
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#1 (permalink) |
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Hey guys wondering if anyone is having problems with their sc stage 1 or 2, at 7100 rpm my boost and power just plummet. It is about *100 whp and +1 lb of *boost of loss every dyno pull and this always occurs *like clockwork at 7100 rpm. Seb and I are racking our brains trying to figure it out. We believe it's a software issue. I believe we are going to send the logs to uprev / Sam on Monday.
Please let me know if anyone has any knowledge / experience / advice. Note: I have a gtm sc stage 2 Last edited by kosstick; 01-28-2012 at 11:00 AM. |
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#4 (permalink) | |
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Updated OP with the kit I have. This issue occurred when we swapped to the ark exhaust from Invidia (which was more restrictive). We have also swapped the pulley to a 92 mm one but the sharp decline started once the exhaust was swapped out. |
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#5 (permalink) | |
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did you retune it after the pulley change though? |
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#6 (permalink) | |
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We went from 460 whp peak to 340 And then it shows to start building up power again |
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#7 (permalink) |
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I dunno. When I first bolted on the ARK Grip exhaust there was no dramatic reduction, although from a nearly flow through GTM exhaust to that, I did not feel a gain. Possibly a slight loss, but not 100 whp, and they were able to tune it back up. We did not do a back-to-back.
That said, a drop of this caliber sounds very much like a fuel cut in some form. One of the better changes I made was when I asked Sam to raise the fuel cut (RPM limiter in effect) to 7800 RPM from 7500. The car wanted that extra and it used it. He did NOT want to go this high, but I assumed all responsibility. Got a graph? Coop
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Jim Cooper - (Retired: '08 Infiniti G37 Sport • TheShopCT built • 11.13 @ 123 mph (click for vid) • GTM Stage II Twin Turbo • 5-speed A/T Level Ten built • 591whp @17 lbs boost) |
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#8 (permalink) |
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It would help if you data logged via UpRev so that you can determine what your MAF is reading , timing adjustments, as well as what your A/F ratio is reading. Two things come to mind; one that a coupling is leaking and a less restrictive exhaust or even a major exhaust leak could be the cause. But a 100 HP loss is staggering and I would expect something else related to the A/F ratio. First things is to datalog, as the data will always show the problem.
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Is your transmission or torque convertor shot?
I assume you have a automatic transmission. + or - 0.5 volts on your MAF air flow is a huge difference. Expecially with the 3" intake piping. Plus if your boost is low, I would automatically be looking for a boost/vacumn leak in your couplings/connections or the boost relief valve could be sticking.
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