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SharpByCoop 09-06-2010 10:34 PM

Subscribed... :)

I also have a 2008 G37S, and I'm about to order the same kit. Looking forward to continued results. I have an auto and so I'll need a few supporting mods in that department, but it sure sounds like it's a go. Thanks for the post. :tiphat:

Regarding the Synchronic BOV: I had a Synchronic on my Subaru STI and after changing and futzing with settings, it worked PERFECTLY. Yes, there are a few adjustments, and you DO need to plumb back into the intake, especially with the MAF. It is quieter if you do so, too. (For me: A good thing. Others: Not so important)

The low throttle response was immediate and gave zero flutter, which I couldn't lose with the TIAL. I'd be giving those a try once again. Glad to know the TIALS are OK, though.

Don't know anything about the other brand.

Jim

Greedy 09-06-2010 10:48 PM

Quote:

Originally Posted by WarmAndSCSI (Post 710054)
lol Lou, I knew you'd have something to say.

I like(d) them as well, but it's common-accepted truth that they're not healthy for high-volume turbochargers or even some stockers - they cause unnecessary compressor surge/flutter in some applications, and quite often leak under high boost.

2 SSQV's is actually a really good setup to eliminate flutter and surge (plus it sounds bad ***), but I'd still rather have something else if I were parting together a kit.


My point is: Synapse Synchronic BOV's are indeed legit. I wouldn't call them an HKS knock off at all.

I have the Synapse bov's and another set of upper charge pipes with the Synchronic flange welded on, so I am going to try them again either with the anti-stall kit or recirculated. I am getting a little compressor surge at very low boost levels. I am going to try to adjust the tial's first and see what happens.

WarmAndSCSI 09-06-2010 11:00 PM

Quote:

Originally Posted by Greedy (Post 710092)
I have the Synapse bov's and another set of upper charge pipes with the Synchronic flange welded on, so I am going to try them again either with the anti-stall kit or recirculated. I am getting a little compressor surge at very low boost levels. I am going to try to adjust the tial's first and see what happens.

There should be no need to recirc; your setup is a blow-through hot-wire MAF setup and your BOV's are prior to the MAF. It might just take some adjusting and whatnot - I know the Synchronics are picky about the vacuum line plumbing.

Greedy 09-07-2010 11:13 PM

Here's a few more shots from the trip....

HKS EVC Boost Controller
http://inlinethumb52.webshots.com/44...600x600Q85.jpg

Vegas and Salt Lake
http://inlinethumb52.webshots.com/35...600x600Q85.jpg
http://inlinethumb19.webshots.com/24...600x600Q85.jpg

fstrnldr 09-10-2010 02:12 AM

Quote:

Originally Posted by Greedy (Post 710092)
I am getting a little compressor surge at very low boost levels.

Let me guess this happens at very light throttle as well?

Greedy 09-10-2010 09:17 AM

Quote:

Originally Posted by fstrnldr (Post 715224)
Let me guess this happens at very light throttle as well?

No - none when any throttle is applied. Just when in first or second and getting up to about 1-2 psi at 3k then shifiting. It's only a quick, momentary flutter that sounds like a little surge. Any more rpm's or boost and it blows off completley.

SharpByCoop 09-11-2010 10:55 AM

I am not familiar with the spring tuning on the Tial's, but I understand that's a source to look into for the cure.

That flutter was consistent and annoying on my Subaru with a Tial, and my experience with the Synchonic ended up curing that. 95% of the time we are at low throttle and boost.

Looking forward to your experiences. Thanks for the updates.

Coop

tsui_san 09-16-2010 01:08 PM

Subscribed for results! Would love to get more info on the intake manifold.

Red__Zed 09-16-2010 08:35 PM

Quote:

Originally Posted by SAM@GTM (Post 708519)
Just a little update, he has been on the roed for the last couple days, posted this yesterday on the G37 board .




And here is the before and after dyno


Nice number!:happydance:


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