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-   -   Topgunz - air to air upgrade (http://www.the370z.com/forced-induction/110925-topgunz-air-air-upgrade.html)

redondoaveb 10-05-2018 02:24 PM

Quote:

Originally Posted by wideglideleon (Post 3790397)
I have one. I got from TopgunZ.

Thanks, I'll talk to Aaron

wideglideleon 10-05-2018 03:42 PM

I have his old one, actually his whole system he had on his Z. I'm not using the brace make me an offer!

redondoaveb 10-05-2018 05:16 PM

Quote:

Originally Posted by wideglideleon (Post 3790416)
I have his old one, actually his whole system he had on his Z. I'm not using the brace make me an offer!

I sent you aPM

redondoaveb 10-05-2018 07:58 PM

Belt slippage?
 
1 Attachment(s)
What the heck is wrong here? 928 impeller, 9lb pulley, 2.85 sc pulley, 3.47 jackshaft pulley. 91 octane. Does it look like belt slippage or ?

cupcakez 10-05-2018 08:00 PM

Wow. Scary. I hope mine isnt that low when i dyno it

You have any supporting mods or kits to eliminate the slippage or its just as u say it is?

redondoaveb 10-05-2018 08:08 PM

Quote:

Originally Posted by cupcakez (Post 3790456)
Wow. Scary. I hope mine isnt that low when i dyno it

You have any supporting mods or kits to eliminate the slippage or its just as u say it is?

High traction pulleys. The problem is the way the power drops off so early.

TopgunZ 10-05-2018 09:28 PM

So you were making almost 600whp but then that changed? Wierd. When did it change? Was it sudden or slowly get worse?

redondoaveb 10-05-2018 09:54 PM

Quote:

Originally Posted by TopgunZ (Post 3790464)
So you were making almost 600whp but then that changed? Wierd. When did it change? Was it sudden or slowly get worse?

This is a new 91 tune. I was making 586 on e85 and 471 on 91 @13psi with just the 9 lb pulley, the 2.85 pulley and the Si wheel.

This set up is the 928 wheel, 2.85 sc pulley and 3.47 jackshaft pulley @ 14.4 psi. And I only gained 1.5 or so psi by adding the 928 wheel and the 3.47 jackshaft pulley.

More boost, loss of power. The way the power and torque drop off just doesn't look right.

redondoaveb 10-06-2018 01:10 PM

I think I might have an idea what my issue is. The V3 is rated at 52,000 rpm. With my current pulley set up, my sc is spinning at 66,000 rpm. I'm running the turbo guard screen and have an unresticted intake so I know it's not a restricted intake issue. It appears that it might be that the volumetric efficiency is dropping off (air cfm in vs air cfm out).

I'm going to call vortech on Monday and see if they can confirm my suspicions.

I want to give a big thanks to another forum member "Z"en for explaining the basics of volumetric efficiency to me.

URBiN~HURMiT 10-06-2018 10:36 PM

Quote:

Originally Posted by wideglideleon (Post 3790416)
I have his old one, actually his whole system he had on his Z. I'm not using the brace make me an offer!

So you ended up with my Stillen SC'r and the JR Trans sc'r brace ... I was the original owner ... Glad to see it's still going strong !!!

01206 10-12-2018 03:15 PM

after install a2a and 9 lb pulley. the car start then turn off right away. i check everything is fine. fuel pressure 50-60.
do you guys know what it could be?

wideglideleon 10-12-2018 03:43 PM

Check your wiring , mine did that and I had MAF and Throttle cables switched, easy to do at the end of a long day.

redondoaveb 10-12-2018 04:40 PM

1 Attachment(s)
Super Vortech upgrade, 3.47 jackshaft pulley sc side, 3.00 sc pulley, Tial wastegate and Greddy Profec results on e85.
Only issue I'm having is that Seb had to do about 50 dyno pulls due some other issues and he said that my sc oil is black. Any ideas? Normal break in after rebuild? Supercharger going out, crappy rebuild? I'm going to change the oil and monitor it to see if it continues or if the sc starts making noise.

G3RSTY7 10-12-2018 05:48 PM

Quote:

Originally Posted by redondoaveb (Post 3791936)
Super Vortech upgrade, 3.47 jackshaft pulley sc side, 3.00 sc pulley, Tial wastegate and Greddy Profec results on e85.
Only issue I'm having is that Seb had to do about 50 dyno pulls due some other issues and he said that my sc oil is black. Any ideas? Normal break in after rebuild? Supercharger going out, crappy rebuild? I'm going to change the oil and monitor it to see if it continues or if the sc starts making noise.

Hey you did it, congrats! So switching from 2.85 sc to 3.0 fixed it?
Speaking of noises, anyone have a heavy load sound coming from front of car/blower when reversing? Especially cold. Didnt have that sound before blower rebuilt/no slip kit installed

"Z"en 10-12-2018 06:32 PM

Quote:

Originally Posted by redondoaveb (Post 3791936)
Super Vortech upgrade, 3.47 jackshaft pulley sc side, 3.00 sc pulley, Tial wastegate and Greddy Profec results on e85.
Only issue I'm having is that Seb had to do about 50 dyno pulls due some other issues and he said that my sc oil is black. Any ideas? Normal break in after rebuild? Supercharger going out, crappy rebuild? I'm going to change the oil and monitor it to see if it continues or if the sc starts making noise.

Beautiful!!


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