Originally Posted by hc_416 Hey guys, Was back at it again. After i got the pump off i took the bottom plate off to see what happened. I see no
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12-22-2018, 08:33 PM | #481 (permalink) | |
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Those gears look mint. Did you pull the gears out at all? If the motor is running there is absolutely no reason for a rebuild. I have never seen one of these fail.
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12-23-2018, 10:18 AM | #482 (permalink) | |
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12-23-2018, 12:55 PM | #484 (permalink) |
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Never bothered. In my case it was post popping the motor. I had small debris inside but nothing big. However seeing my oil pan I can guess that something big may have gone through. My problem was a circlip. But the pump itself is a good product. The worst oversight I made was not getting an inline filter to save it. The inlines were on their site. With my new one it runs like a top and I think the other one would've too barring me blowing the motor. |
12-23-2018, 01:29 PM | #485 (permalink) | |
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Mine came with an in-line strainer |
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01-21-2019, 10:50 PM | #490 (permalink) | |
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I’ve never taken one apart, but dumb question, is the spring out of it? |
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01-22-2019, 01:15 AM | #491 (permalink) |
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Unless the gate is malfunctioning, there is really no reason to take it apart. Once the crews are out, there is nothing else holding the top cap in place. So be careful as the spring can send things flying once it does become loose.
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01-22-2019, 03:34 PM | #492 (permalink) |
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Now that were on the topic of wastegates.. I'm still having overboosting/boost creep issues. I spoke with my tuner and he sent me an updated map. Fixed the problem for a day and then started overboosting the next. I know it's not a cold weather issue because its been happening all year.
I've seen alot of other platforms having boost creep issues with the external tial wastegates. I could be going down the wrong path here but has anyone swapped to a different wastegate completely and has anyone else had this issue? I spoke to solidus about this and he said his wastegate spring pressure was not rated for what tial claimed when tested. Even if that's the case. Shouldn't the tuning keep the boost pressure from going over? I'm not the most knowledgeable when it comes to turbochargers so I'd appreciate any help or advice I'm having a vacuum pressure test done just to rule out any type of vacuum leak.
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01-22-2019, 03:36 PM | #493 (permalink) | |
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01-22-2019, 04:01 PM | #494 (permalink) |
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The springs test + or - 1 to 2psi. What Realstreet does is test each spring they install to match the rates. As far as taking the wastegates apart I use a C-clamp then slowly release it. Unless you want to see parts fly. Put it back together the same way to avoid crossthreading.
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01-22-2019, 06:21 PM | #495 (permalink) |
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I have not. Tomorrow I'm bringing it to shop for a vacuum pressure test. Might as well have them take a look while its there.
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