So I got the 9lb pulley on with the roller back in the right spot, replaced the OEM tensioner and installed the new belts. No evidence of anymore belt slippage but still only getting about 10 psi of boost. Did a boost leak test and found a few loose clamps that were losing a little air. Tightened all of those. The only other leak I found was at the Mass air flow sensor. Extremely slight leak due to a stripped bolt. Will have that taken care of once I get it back to RT Tuning. At this point I'm wondering if it needs a new tune due to the pulley change. Any advice always appreciated.
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TopgunZ C38R SC // Rotrex // CJM // ID 1340cc // Walbro 525 Hellcat // Ecuteck // 4 Bar Map Sensor // Z1 Oil Cooler // Tial // Prosport JDM // South Bend Stg 3 // ACT // RT Tuning Install and Tune // Motordyne ART // Berk CBE // Michelin PS4S 305/30/19R 265/35/19F
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