Its actually a innovate SCG-1. I'm not 100% what solenoid it is but it is still on the car. After reading more threads and remembering my EBC didnt work properly. I'm beginning to think that this is a plumbing issue. I plumbed in the vacuum lines per sashas instruction manual. I had a shop do the boost controller plumbing after. I'm wondering now if the reason my tuner could never get it to function properly was because it was plumbed incorrectly. Still somewhat abnormal considering the car ran great for a while after it was tuned. If the WG springs and 02 sensor doesnt cure my boost creep problem I might just have the boost controller solenoid removed and the plumbing completely redone.
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Boosted Performance Single Turbo
618whp/489 tq
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