Quote:
Originally Posted by ANMVQ
Hey Jay ,
incase we forgot my story as it was a few years ago.
What was the WHP? 465
What wtrq? 330
How long did it run before it died? 3DAYS!!!
Was it ever 100% running right before it died? Yes, long story
What kit? Stillen SC
What PSI? 13 PSI
What was the cause if you know? Cyl 3 went bye,
What year was the car? 2011 G37X Coupe
Long story was a drove the car for 6 months @ 412 WHP and 300WTRQ, had some issues with the SC ingesting water, then TB harness broke, fuel pump feed line split cause it was wrong. Pretty much all this happened the same time. So I upgraded the impeller and got a retune from Kaizen. The car ran great for 3 days the blew up.
Not to revisit the whole story but I think the tune was part of the issue on top of the tuner making multiple WOT pulls on the dyno and telling me the car is way down of fuel. They probably could have diaq'd it better and making WOT pulls before finding the feed line was split to the fuel pump. Hell I suggested that over the phone after they had the car for like 2 weeks!
I also upgraded everything under the sun and still failed
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I asked this question in 2014 and unfortunately I joined the club of blown motors this year! Was your tuner named Rob by chance?
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